You can watch a full video version with more details here.
I decided to try and do a nicer repair than the previous effort.
Last time, worked, but it was a bit of a mess. This time, I made an effort to match the bodge wire to the right shape and length.
I also tinned the ends of the enamel coated wire. This does require quite a bit of heat, I turned my soldering iron up to 400C. This made things a lot easier.
The only slight mistake I made was in the final cleaning - I was a bit too aggressive and ended up moving the wire about quite a bit.
However, the end result - once it’s covered in solder resist - is a lot nicer.
I think I’m getting better at this!
Have a watch of the video and let me know what you think!
Easy 8.8 Amp Power Supply Hook Up - But is it safe? - In this DIY assembly venture, I decided to tackle the challenge of designing a safer casing for the bare, open mains connections on my LRS-200-24 power supply. To add to the challenge, the connector size was surprisingly wide and deep, which created hurdles in 3D printing the perfect box. I tried several renditions, from printing in separate parts to changing the design into a tubular construction, but these ventures resulted in a bit of a printing scrap heap. After discovering a sturdy, push-fit, slimmer connector online, my 3D printing journey went a little smoother, resulting in a front panel that slid nicely onto the power supply unit. The project also involved some dexterous wire threading, soldering, securing switches, and sockets, and accommodating everything within the newly printed enclosure. An exciting yet fiddly bit of work, it has come along quite promisingly – a test run confirms functionality. On the agenda for the next round – possibly extending the enclosure for some more elbow room for the wires. Definitely been a 'shocking' fun electrical endeavour!